Late in the afternoon I woke up feeling well enough to do some
hardware work. I'd been considering whether to populate and test another
small section of the Instruction Pointer board, or just do the rest of
the board in one marathon session. Experiments suggested that if I
populated much more I wouldn't be able to use the solder stencils for
the rest, which sort-of settled the issue.
At about 6pm
I used the stencil to put solder paste on as much of the board as I
could, then started placing components. At first this was slow, but
eventually I developed a fairly efficient rhythm. Still, I had a bit
more than half the board to populate, or about 300 parts to place. It
took me about four hours, by which the solder paste had mostly dried
out, so rather than the components settling into the paste like a foot
into soft mud, they sat on top. I was rather worried that even with a
low airflow, the hot air soldering wand would blow components away
before the solder paste reflowed. Indeed, this happened with a few
components, but most stayed in place.
Reflow soldering
has to be seen to be appreciated. The dull-gray solder paste suddenly
turns bright silver, and misshapen smears suck together like a scene
from the Terminator 2 movie. Components that are slightly misaligned
rise and twist into alignment, then settle to sit flat on the board. It looks like animation, but it's surface tension in action.
And
then there are the failures. Resistors rise on one end
until they look like partly-raised drawbridges, a condition aptly named
"drawbridging", or until they're completely upright, known as
"tombstoning". Transistors rise on one lead, looking like an acrobat
balancing on one arm. All these have known causes, mostly related to
poor solder paste application or uneven heating, both offenses I'm
horribly guilty of committing. A couple components simply flew away,
like a speck of dust blowing in a gust of wind and barely perceptible
until a careful inspection shows a couple of empty pads where there
should be a resistor. There's a reason I bought 100 extra resistors.
I think for the next board I'll just populate the whole thing at once, which will minimize my problems with the stencils. I may also try the hot plate method of reflow, which gives a more even temperature distribution and avoids blowing components away.
With
the missing components replaced and the soldering problems fixed, I
checked for major problems (like a short between the +5V and Ground
buses). Not finding any real problems, I plugged the thing into my test
jig. My simple test driver doesn't give a real test, but the few signals
I probed looked reasonable.
By this point it was midnight, and I crawled off to bed.
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